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· Banned
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7,730 Posts
Discussion Starter · #1 ·
Just wanted to voice the fact that I ran the BD short throw shifter this entire week since last saturday and was never more impressed with ease of shifting and control as when I put the STOCK assembly back in yesterday...

Upon installation I refused to even use the hardware that came with the kit. I instead used some class 12 recessed allen head bolts identical to the OEM pieces except obviously in length. It came with maybe grade 5 hex head bolts with cheezy washers under the heads. Theres no room for that bs next to the tower (not comfortably) and besides, I could just see one of those breaking off in the transmission case. Not to mention the "That just looks cheese-dick" aspect that I wasn't willing to accept.

Anyway, no big deal, swapped out the hardware and it went in fine.

Problem is, it moved the damn shifter up about an inch :eek:. That's real professional. Totally threw off the ergonomics of the shifter. So you imediately feel like you just sat down in an OTR tractor, or an old dumptruck.....not exactly performance inspiring to say the least.

But the biggest issue was the fact that it shifted like crap. The shifts felt like crap, and the shifting effort made it feel even worse. Obviously this is due to the sacrificed leverage for the sake of increased travel speed.

Basically, if they had wanted to do this right they wouldn't have changed the ratio that far (too hard to shift, and pattern was actually too tight for a big tranny to work properly) and they would have SHORTENED the damn shaft accordingly. OR.....for damn near 300 bucks they could include a new freakin shifter lever altogether.

Not well designed, although other than the issue with the chezzy hardware, it was well made.

Just wanted to get that out there in case anyone else might be swayed to give it a try as well.

Stock assembly is 300% smoother and more controllable IMO.

Two Cents
 

· Cummins Power
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3,082 Posts
I've thought about this mod for a while. I think you just saved me some money.
 

· Jaw-Juh Stroker
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91 Posts
Yeah I was thinking about it too for a long time, and I'm glad I haven't acted on it.

Really, the stock shifter ain't half bad, and I couldn't justify shelling out cash just so I could move the handle a little less.

Thanks for the review.
 

· Banned
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7,730 Posts
Discussion Starter · #6 ·
I would have saved some money I guess, but if it is truly the same thing, then at the end of the day I would simply have a 185 dollar POS rather than the 289 dollar POS that I have now because it's not worth having no matter the cost.

Or to put it another way.....if you would pay me 300 dollars to put it in and leave it, I would tell you to screw yourself, lol.
 

· I love you bigrpowr!
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1,183 Posts
LOL

I have never seen or driven in a truck with one but all the reviews other than this one I have read are positive. Then again, maybe your used to the real short shifters like I am that you put in most any sports car. They are purpose built and do not just raise the shifter to make the movement shorter.
 

· Banned
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7,730 Posts
Discussion Starter · #8 ·
I think it also has to do with them not having the Sac to admit they waisted nearly 300 dollars and wish to hell that they could somehow stomach the idea of actually putting it back to stock and enjoying their tranny once again.

You'd be amazed at the stupid things people will deal with because someone said it is "supposed" to be better than stock.

Early chip "tuning" with the EOT table comes to mind, along with "injector rattle"......cough, cough....blown ass engines with hanus timing.
 
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